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400 exc popping and banging on deceleration

8.8K views 39 replies 11 participants last post by  Lark09  
#1 ·
As above my 400 exc is popping and banging on deceleration. I’ve checked the header to cylinder interface and it all looks good, could the header to silencer joint be the issue? That assumes my assumption of air leak is correct.
The only thing I’ve done to the bike is clean and rebuild the carb and she’s running lovely apart from this popping and banging. I also did the O ring mod on the accelerator pump which has eliminated the bottom end bog.

Any suggestions
 
#7 ·
A guy on an SWM who ride with us on a newly serviced bike yesterday had popping and banging from the exhaust for a while until it finally gave up. The pipe from the throttle to the engine hadn’t been clamped up properly so it was running horrendously lean.

I had a similar thing with a vacuum Scottoiler on an old Triumph that hadn’t been sealed into the manifold properly and some of the overrun explosions were huge.
 
#10 ·
Right, had a good check of the inlet rubber and it looks ok. I’ve reseated it and tightened, still the same.
I think the main jet may be a little rich as my spark plug is a bit sooty. Again it’s stock 178 I think. Needle clip position is in the middle.
I can only assume the pilot jet is ok as it ran ok before, it’s a stock 42. Fuel screw is set at about 1.5 - 1.6 turns so I’ll try with 2 and see what it does. Not the easiest to adjust when engine is hot even with a fancy extended screw. What’s the trick my hands are just too big to get in the space.

I did find the silencer to header joint not quite seating square but its still the same even when realigned.

Could it be ignition timing?

Cheers Lark09
 
#13 ·
So just tried messing with the fuel screw and engine falters at about 1.3 turns out and recovers at about 1.5, I then wound out 2 and there is some improvement in response but still popping a bit. I then went to 2.5 again a little better but was expecting rpm to drop but didn’t then out to 3 turns
No difference. Still popping and response much the same.
So does that mean I’m running on just the jet size with no fuel screw reduction?
My needle is on the middle position which I think is richer than stock.
Do lift the needle up one more or fit a 45 pilot jet?
Unfortunately, the missus was moaning that I was making too much noise so activity curtailed tonight or I would have tried the needle.
 
#15 ·
I’ve had this problem and it can be difficult to solve, I did eventually do it with carb cleaner but in the end it would probably have been quicker to get the carb ultrasonically cleaned.
Anyway
Check all the circuits in the drawing, it’s possible to have the slow jet (pilot jet) clear but the passageway above it or the air supply to it blocked. Sounds like your pilot screw is working ok but the slow circuit not.



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#20 ·
Thanks there’s some good stuff here. I replaced the plug cap about 10 hrs back when I had an issue with the previous one so I doubt it will be that but worth a shot.
The carb was cleaned and rebuilt which is where this all started, there was some muck in it and the float valve seat O ring was leaking so I replaced all the seals. It was ultra sonically cleaned so I would hope it was clean however we all know stuff does get in.

So I will try the needle first and see how we go. Fit new plug cap. If that doesn’t work I’ll strip the carb again and re clean. If that doesn’t work then I’ll try a 45 pilot jet. Then I’m screwed.

By lifting the needle where does it richen? 1/8 upto 1/2 throttle?
As a matter of interest the exhaust is an Ackropovic would that have any bearing on the situation.

Cheers Lark09
 
#21 ·
This will give you a better idea...

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Just make sure you give this part a good clean, it can take a couple of goes to dislodge and dirt or stale fuel.

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Bigger bore and / or more free flowing exhausts can make it lean across the range... Pilot is less sensitive in that regard as long as you get it idling correctly and jetted in the right range for temperature and elevation. Should only ever be a jet size or clip setting from there. Check it again for air leaks when adjusting the clip height (lower - richer).
 
#23 ·
Thanks for the carb info very useful and explains nicely.
I reseated the can /header pipe joint which did make a slight improvement. I am not using any sealant and wasn’t prior to all of this. The joint is held together with a spring.
I did think about using a 50mm O ring in the can/pipe junction but haven’t tried that as yet. Not too sure if the temp might be a bit high. I guess a viton seal would be the best for temp.
My 200 exc exhaust had O rings at the barrel end and worked ok.
I’m away on hols now so I’ll have another go in a weeks time.

Appreciate the help
Lark09
 
#25 ·
You need to be careful with viton o rings, if they melt and the goo then gets on your skin (even when cold) it will eat into your skin, the only way to stop it is to cut the skin away!

Just did a quick google, viton gives off Hydrofluouric acid when burnt.
 
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#30 ·
They may well be made of viton but the whole power valve assembly on the 2 strokes is water cooled which means that the exhaust pipe temperature is going to be much cooler than a 4 stroke exhaust. I'm pretty sure that the actual exhaust gas temperature on a 2t is cooler anyway than a 4 banger.